R792 DHB Volvo B10m 16/12/17 The last job on this bus was to check over for mot and reposition the wiper arms which that was not as simple as it seemed but success was achieved in the end and they now stop in the correct place.
Engineers Corner
R792 DHB Mud flap work – 8/12/17
This weekend we removed damaged rear mudflaps and fitted new ones these will help keep rear of bus clean. Then we fitted rubber packing to tank straps and refitted the fuel tanks back on the bus. We refilled with fuel and restarted bus and checked for leaks all OK. We will now check her over…
R792 DHB Fuel Tank Straps Repair – 2/12/17
After finishing the front suspension we tasked our self with the renewal of the fuel tank straps. This bus has two separate tanks which both needed removal as the supporting brackets were rusted through as well as the straps. After removal it was decided to renew the outer tank brackets but we managed to salvage…
B10m Suspension Work – 17 /11/17
R792 DHB Volvo b10m Both front suspension air bags perished. We had to jack bus body up, deflate bags, remove air filter ducting, pull bags out. We renewed the bags, pistons and top plates as badly corroded, to refit we had to remove front wheels, shock absorber top mounting bolts to get axle down lower…
PAX – 5 .11.17
The rear suspension torsion bar metalastic bushes were worn. We removed the torsion bar from the bus and cut out the old bushes. We are now trying to source new ones.
258 Off The Pits (12.10. 17)
258 left pit today after a lot of mechanical work had been completed, a service and pre MOT check was also carried out. Some seat cushions now need to be re trimmed and a thorough clean of the bus before a mot test.
258 Doors Opening
More progress on 258. The front doors were not opening properly so the fault was traced to the operating valve in the destination box which was leaking air. We had to modify a Dennis dart valve of which we had a good one in stock by altering the pipework to fit. This done we then…
Compressor Work
Having got the right parts, Bob and Mike set about reassembling the compressor and fitting it back into 258. Below is a photo of all the parts on the table prior to being put back into the vehicle. The pink gasket near the camera was the gasket we had trouble sourcing. Below is a photo…
258 Exhaust Work
While awaiting new parts for 25′ s compressor we made a new strap for the exhaust silencer heat shield which had been remade a while ago but not secured to bus.
Compressor work on 258
A job that has been put off for a while was eventually tackled this weekend. Ex Cardiff Lynx (258) has had a compressor head gasket air leak which results in it taking awhile for the vehicle to build up air pressure. This is not a very pleasant job as access to the compressor is not…